Cause Analysis on Pulling out of Import φ339.7 mm Casing Connection in Well Cementing Process
摘 要
对某井进口φ339.7 mm 电阻焊(ERW)套管固井事故进行了全面调查研究,通过对磁性定位测井CCL曲线反映的套管柱失效形貌和对井下捞出的套管残片形貌进行分析认为, 套管柱在固井过程中发生了脱扣, 脱扣位置在第5根套管的工厂连接端。通过对套管的螺纹加工、材料和上扣连接质量等进行分析和对套管柱在固井过程中的受力状态进行计算认为, 套管所受载荷远小于其连接强度, 排除了过载导致套管脱扣的可能性, 认为套管接头是在固井期间首先松动之后才发生脱扣的; 套管接头在井下松动的原因是由于套管柱在固井过程中受到了很大的震动载荷; 套管接头从工厂上扣端松动脱扣的原因主要与工厂上扣扭矩偏小有关。
Abstract
The well cementing accident in one well was comprehensively investigated and studied. It was found that the import casing string was pulled out from the 5th casing mill connection end during well cementing process by analyzing the CCL curve of magnetism orientation survey well and distinguishing casing remains fished out from the well down. The possibility that over load resulting in casing connection pulling out could be eliminated because the load borne on the casing connection was far less than its rated tension strength according to the test results and casing service condition. It was considered finally that the casing connection was unscrewed first due to jarring load borne on it during well cementing because it was not made up with enough torque in the mill, and then was pulled out by analyzing and calculating.
中图分类号 TE931+.2
所属栏目 质量控制与失效分析
基金项目
收稿日期 2010/10/9
修改稿日期
网络出版日期
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备注吕拴录(1957-),男,教授级高级工程师。
引用该论文: LV Shuan-lu,JIA Li-qiang,FAN Wen-gang,ZHENG Xiang-zhong,LV Qing-gang,WEI Shan-quan,WANG Cheng-ming,YIN Xue-dong. Cause Analysis on Pulling out of Import φ339.7 mm Casing Connection in Well Cementing Process[J]. Physical Testing and Chemical Analysis part A:Physical Testing, 2012, 48(2): 130~133
吕拴录,贾立强,樊文刚,郑向忠,吕庆钢,魏善泉,王成明,尹学东. 进口φ339.7 mm套管在固井过程中脱扣原因分析[J]. 理化检验-物理分册, 2012, 48(2): 130~133
被引情况:
【1】潘志勇,韩新利,王新虎,王建东,李东风,朱丽霞,刘心可, "某油井圆螺纹套管接头脱扣原因分析",理化检验-物理分册 51, 143-146(2015)
【2】张钧,赵国仙,吕祥鸿,宋文文, "塔里木油田某井油管脱落原因分析",理化检验-物理分册 50, 845-848(2014)
【3】吕拴录,腾学清,李中全,杨成新,李宁,文志明,徐永康,石桂军,杜涛,王俊友, "钻具提升短节脱扣分析及标准化",理化检验-物理分册 52, 36-38(2016)
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参考文献
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【2】API SPEC 5B:2004. Specification for threading,gaging,and threaded[S].
【3】API BUL 5C2:1999. Bulletin on performance properties of casing,tubing and drill pipe[S].
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【6】吕拴录. φ139.7 mm×7.72 mm J55长圆螺纹套管脱扣原因分析[J]. 钻采工艺,2005,28(2): 73-77.
【7】袁鹏斌, 吕拴录, 姜涛, 等. 长圆螺纹套管脱扣原因分析[J]. 石油矿场机械,2007,36(10): 68-72.
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【2】API SPEC 5B:2004. Specification for threading,gaging,and threaded[S].
【3】API BUL 5C2:1999. Bulletin on performance properties of casing,tubing and drill pipe[S].
【4】茅春浦. 流体力学[M]. 上海:上海交通大学出版社,1995.
【5】LV Shuan-lu,HAN Yong,QIN Chang-yi,et al. Analysis of well casing connection pullout[J]. Engineering Failure Analysis,2006,13(4):638-645.
【6】吕拴录. φ139.7 mm×7.72 mm J55长圆螺纹套管脱扣原因分析[J]. 钻采工艺,2005,28(2): 73-77.
【7】袁鹏斌, 吕拴录, 姜涛, 等. 长圆螺纹套管脱扣原因分析[J]. 石油矿场机械,2007,36(10): 68-72.
【8】吕拴录,宋治. J值在API圆螺纹连接中含义初探[J]. 石油钻采工艺,1995(5): 56-62.
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