Cause Analyses of Pin Joint Fracture of 139.7mm Heavy Weight Drill Pipe
摘 要
为查明某井139.7 mm加重钻杆外螺纹接头的断裂原因,对断口进行了宏观和微观分析,对材料进行了化学成分分析、力学性能试验和金相分析,并进行了有限元分析等.结果表明:加重钻杆断裂属于腐蚀疲劳断裂;断裂主要原因是加重钻杆接头内径大于标准规定值,降低了加重钻杆外螺纹接头断裂扭矩和抗拉载荷,在疲劳载荷与腐蚀介质作用下,腐蚀疲劳裂纹首先在加重钻杆外螺纹接头危险截面部位螺纹牙底萌生,随后在载荷作用下裂纹不断扩展,进一步降低了接头的强度,最终发生了断裂事故.
Abstract
For investigating the failure causes of pin joint fracture of a 139.7 mm heavy weight drill pipe,macro and micro analyses of the fracture surface were carried out.And the material chemical composition analysis,mechanical property test,metallography and finite element analysis were performed.The results show that the pin joint fracture of heavy weight drill pipe was corrosion fatigue failure.The tensile strength and torsion strength of the heavy weight drill pipe pin joint were reduced because its inner diameter was bigger than that specified in the standard,which led to the fracture.Under fatigue load and corrosion medium,corrosion fatigue crack appeared first at the bottom of thread which was the dangerous section part of the pin joint.Then the crack grew constantly under the loading and further reduced the joint strength,which led to final fracture.
中图分类号 TG115
所属栏目 失效分析
基金项目
收稿日期 2008/9/18
修改稿日期 2009/4/8
网络出版日期
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备注吕拴录(1957-),男,陕西宝鸡人,教授级高级工程师.
引用该论文: Lv Shuan-lu,JI Bing-yin,LUO Fa-qian,KANG Yan-jun,ZHANG Qi,FENG Shao-bo,LI Jin-feng. Cause Analyses of Pin Joint Fracture of 139.7mm Heavy Weight Drill Pipe[J]. Materials for mechancial engineering, 2009, 33(10): 99~102
吕拴录,姬丙寅,骆发前,康延军,张琦,冯少波,李金凤. 139.7mm加重钻杆外螺纹接头断裂原因分析[J]. 机械工程材料, 2009, 33(10): 99~102
被引情况:
【1】袁鹏斌,吕拴录,许峰,余世杰,文志明,历建爱, "AT-16井钻杆NC50内螺纹接头胀大原因分析",理化检验-物理分册 50, 457-460(2014)
【2】黄本生,卢东华,姜涛,张俊,宁扬忠, "G105钻杆在不同氢离子浓度溶液中的腐蚀行为",机械工程材料 38, 81-84(2014)
【3】吕拴录,龚建文,卢强,迟军,许峰,张国正,张春婉, "提升短节外螺纹接头断裂原因分析",机械工程材料 35, 86-88(2011)
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参考文献
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【3】吕拴录,高林,迟军,等.石油钻柱减震器花健体外筒断裂原因分析[J].机械工程材料,2008,32(2):71-73.
【4】Lv Shuan-lu,FENG Yao-rong,ZHANG Guo-zheng,et al.Failure analysis of IEU drill pipe wash out[J].Fatigue,2005,27:1360-1365.
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【6】吕拴录,骆发前,高林,等.钻杆刺穿原因统计分析及预防措施[J].石油矿场机械,2006,35(增刊):12-16.
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