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油田井控装置放喷管线的爆裂原因
          
Cause of Bursting of Choke Line in Oilfield Well Control Device

摘    要
某油田油井在实施侧钻过程中其井口放喷管线发生爆裂,通过宏观形貌观察、无损检测、化学成分分析、力学性能测试、断口形貌观察等方法以及爆裂放喷管线的抗内压强度校核,分析了该放喷管线发生爆裂的原因。结果表明:该放喷管线在本次使用前对存在轴向穿透裂纹的外壁进行过补焊处理,但补焊焊缝厚度很小,远小于管线壁厚,导致管线承压能力不足而在侧钻过程中发生爆裂失效,同时管线较差的韧性和冲击性能促进了脆性断裂的发生。
标    签 井控装置   放喷管线   爆裂   管道修复   well control device   choke line   bursting   pipeline repair  
 
Abstract
The choke line of an oil well in an oilfield bursted during the sidetracking process. The reason for bursting of the choke line was analyzed by macromorphology observation, non-destructive testing, chemical composition analysis, mechanical performance testing and fracture morphology observation, as well as internal pressure resistance checking of the burst choke line. The results show that before being used this time, the external wall of the choke pipeline with axial penetration cracks was repaired by welding treatment. The thickness of the repairing weld was very small, and much less than pipeline wall thickness, resulting in the bursting failure during sidetracking because of insufficient bearing capacity of the pipeline. Meanwhile, the poor toughness and impact performance of the pipeline promoted the occurrence of brittle fracture.

中图分类号 TE988.2   DOI doi: 10.11973/jxgccl202303017

 
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所属栏目 失效分析

基金项目 国家重点研发计划项目(2017YFC0805804)

收稿日期 2022/1/16

修改稿日期 2023/2/6

网络出版日期

作者单位点击查看

备注王帅(1986-),男,山东淄博人,高级工程师,硕士

引用该论文: WANG Shuai,ZENG Jiang,ZHANG Zhimeng,SONG Jie,ZHANG Shuxin. Cause of Bursting of Choke Line in Oilfield Well Control Device[J]. Materials for mechancial engineering, 2023, 47(3): 98~102
王帅,曾江,张志猛,宋劼,张庶鑫. 油田井控装置放喷管线的爆裂原因[J]. 机械工程材料, 2023, 47(3): 98~102


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